A supreme bridge can be defined as
a bridge that can support a large amount of weight at a low cost. That was the goal for this class. Our job was to build the best bridge possible
using K’Nex pieces. A truss is a
triangular joint that disperses weight.
Most bridges today are built with some sort of truss system. Each week we were given a different
assignment regarding bridges. Throughout
this course we would use software, online resources, pencil and paper, K’Nex
and our minds to design a bridge. Westpoint Bridge Designer is a popular
bridge-design program that allows the user to create their own bridge and test
it. The program displays results in the form of compression and tension forces
acting on the designed bridge. Bridge Designer was also used. This program focuses heavily on forces of
tension and compression acting on a bridge that the user sketches. One could also analyze forces acting on a
bridge using the “Methods of Joints”.
This process requires the use of physics to calculate forces acting on
joints. The first bridge that needed to
be built had to be at least two feet long.
This allowed us to get in some good bridge building experience before we
started on our final design. While
building, it was suggested that cost be kept in mind because the cost to weight
ratio is what the final bridge’s effectiveness will be determined by. After the two-foot bridge was built, the next
task was to construct a three-foot bridge.
This time, the bridge had to have a two-by-three inch hole running through
the middle. This constraint was
implemented to simulate the construction of an actual bridge in which a
passageway for transportation was necessary. As the term went on, each group
member was responsible for posting entries on the team blog weekly. These posts would answer a question determined
by the professor each week and recap what had happened in or out of class during
the previous week.
From the
beginning, the goal was to build a strong bridge and brainstorm ways to make it
less expensive. The team favored this
approach because there was always a way to make the bridge support more weight
and there were always ways to make the bridge less expensive. This was not the most efficient approach
because supporting the most weight does not always result in the best
bridge. The best way to build a bridge
is to consider factors such as cost and strength, in the design planning. To achieve success other small goals were
set. The team planned on meeting weekly to
discuss our plans while moving further.
This was a good idea because it gave each member more time to
brainstorm. Another goal was to listen
to and consider every idea. When conflicting
ideas arose, compromising is always the most effective solution. Every goal that was established early in the
course was met even though the final bridge outcome was somewhat of a
disappointment. The goal to build the
strongest bridge possible and disregard cost was the only goal that was altered
in the building process. This method was
abandoned because it would severely alter the cost-weight ratio and one design
mistake could result in an unfavorable, high ratio. Our first bride design was
ridiculously expensive. More
specifically it was the most expensive in the class. This is the point where our goal
changed. For the second bridge design,
which was the three-foot design, we had made cost efficiency a main priority
along with strength. The role of
individual assignments was very helpful when compiling the final design. These assignments made the group come up with
as many bridge designs as possible so that best design could be chosen. These assignments also help us get a better individual
understanding of bridge design. Westpoint Bridge Designer helped each
member achieve a better understanding of what designs worked the most
efficiently and which ones did not. The
force analysis and calculations brought to attention where significant force
was being applied the most and where it was being applied the least. The program also challenged each member to
try and make an inexpensive bridge while also maintaining the bridge’s safety. When the truss analysis was carried out, it
again revealed areas on the bridge supporting large amounts of tension and
compression. In addition to using the
program, each member also carried out calculations done by hand. Each member’s individual designs produced the
widest range of ideas. This was helpful
because the team was able to see which design was the most effective, then
improving on the chosen design. After testing
the original bridge design, the structure bowed and the bridge failed. When it was time to build the final bridge, the
two most important objectives in mind were cost and failing weight. The original bridge was incredibly expensive
due to the large amount of pieces used.
To lower price, the team used longer members and fewer gusset plates. The
three-foot-long final bridge ended up costing as much as the original two-foot
bridge. To avoid the bridge failing due
to bowing to the side, additional trusses were placed in the center of the
bridge. At first when the final bridge
was tested, it did not hold as much weight as was hoped. As a result, an additional truss section was
added to the top of the bridge for added stability. This change resulted in the bridge’s ability
to support another ten pounds. The final
design resembled a series of attached cubes with a top truss section. The sides had trusses resembling X’s, held
together by members that were perpendicular to the sides and trusses in the middle. The predicted load at failure for the final
bridge was about forty pounds.
Figure 1: Truss Analysis |
Figure 2: Bridge Designer |
Figure 3: Westpoint Bridge Design |
The three-foot bridge design was
approached in a similar way as the two-foot bridge, except for minor changes to
reduce cost. All grooved gusset plates were removed to significantly reduce
overall cost. The design began as a simple truss bridge with X-shaped supports
on the sides and an over truss section for added support. The bridge continued
to be less stable than desired. Because of this, more pieces were added to the
center. These added supports resulted in the doubling of the overall amount of
weight the bridge was able to support.
Bill
of Materials - Knex Pieces
|
|||||||
Part
Number
|
Description
|
Unit
Cost ($)
|
Nr. of
Parts
|
Cost
($)
|
|||
1
|
1.25"
long chord
|
$500
|
56
|
$28,000
|
|||
2
|
2.125"
long chord
|
$1,000
|
108
|
$108,000
|
|||
3
|
3.375"
long chord
|
$1,500
|
80
|
$120,000
|
|||
4
|
5"
long chord
|
$2,000
|
10
|
$20,000
|
|||
5
|
7.5"
long chord
|
$3,000
|
0
|
$0
|
|||
6
|
chord
splice
|
$1,000
|
0
|
$0
|
|||
7
|
45
degree gusset plate
|
$1,000
|
0
|
$0
|
|||
8
|
90
degree gusset plate
|
$1,000
|
0
|
$0
|
|||
9
|
135
degree gusset plate
|
$1,000
|
0
|
$0
|
|||
10
|
180
degree gusset plate
|
$1,000
|
108
|
$108,000
|
|||
11
|
180
degree grooved gusset plate
|
$2,000
|
0
|
$0
|
|||
12
|
360
degree gusset plate
|
$1,000
|
0
|
$0
|
|||
13
|
360
degree grooved gusset plate
|
$2,000
|
0
|
$0
|
|||
Total Cost
|
$384,000
|
Figure 4: Bridge Sketch |
Figure 5: Final Design |
The bridge failed around 31 pounds.
Instead of exploding into thousands of pieces, the bridge bowed out to the
side. The bridge broke on the right side under the raised truss section, just
as predicted. In a real life situation this would be preferred because bridge maintenance
would be easier. Inspectors would know where to look if the bridge was failing.
Figure 6: Breaking Point |
Figure 6.1: Breaking Point |
After testing the final, three-foot
bridge, it was determined that the bridge was able to support 42.3 pounds. The
maximum amount of weight the bridge could support was tested by suspending a
bucket from the center of the bridge and gradually filling it with sand. This
is a far better result than what was originally predicted. During testing, the
bridge failed on the right side directly beneath where the additional truss
section ends. Calculations were made for find the compression and tension
forces acting on the bridge when weight is added. These calculations were used
to predict where the bridge would most likely fail. In conclusion, the maximum
weight of 42.3 pounds was a very successful, unexpected result.
If we were
to design another bridge in the future, we would not make any major changes. We
are very happy with our final bridge result. However, if we wanted to save
money and reduce the overall cost, we could remove some members of the bridge
that are not as essential to the bridge’s strength. Another way to cut down on
the bridge’s overall cost would be to remove some gusset plates. Our bridge has
a lot of joints, I we took out some of these gusset plates, our overall price
would be significantly less but so would the amount of weight the bridge can
support. If our goal were to increase the amount of weight the bridge is able
to support, our main focus would be to add more members. With more members on
the bridge, the weight it is supporting will be dispersed among more supports,
reducing the total amount of tension and compression on each support.
No comments:
Post a Comment